summaryrefslogtreecommitdiffstats
path: root/arch/arm64/boot/dts/rockchip/rk3328-rock64.dts
diff options
context:
space:
mode:
authorKamil Trzciński <ayufan@ayufan.eu>2018-01-22 18:46:22 +0100
committerHeiko Stuebner <heiko@sntech.de>2018-02-12 09:39:01 +0100
commit73e42e18669934fa96cf2bb54291da54177076d7 (patch)
tree9fda71b7be4473f202fca7876047d4c1e7daa94d /arch/arm64/boot/dts/rockchip/rk3328-rock64.dts
parent7928b2cbe55b2a410a0f5c1f154610059c57b1b2 (diff)
downloadlinux-stable-73e42e18669934fa96cf2bb54291da54177076d7.tar.gz
linux-stable-73e42e18669934fa96cf2bb54291da54177076d7.tar.bz2
linux-stable-73e42e18669934fa96cf2bb54291da54177076d7.zip
arm64: dts: rockchip: fix rock64 gmac2io stability issues
This commit enables thresh dma mode as this forces to disable checksuming, and chooses delay values which make the interface stable. These changes are needed, because ROCK64 is faced with two problems: 1. tx checksuming does not work with packets larger than 1498, 2. the default delays for tx/rx are not stable when using 1Gbps connection. Delays were found out with: https://github.com/ayufan-rock64/linux-build/tree/master/recipes/gmac-delays-test Signed-off-by: Kamil Trzciński <ayufan@ayufan.eu> Signed-off-by: Heiko Stuebner <heiko@sntech.de>
Diffstat (limited to 'arch/arm64/boot/dts/rockchip/rk3328-rock64.dts')
-rw-r--r--arch/arm64/boot/dts/rockchip/rk3328-rock64.dts7
1 files changed, 3 insertions, 4 deletions
diff --git a/arch/arm64/boot/dts/rockchip/rk3328-rock64.dts b/arch/arm64/boot/dts/rockchip/rk3328-rock64.dts
index 3890468678ce..28257724a56e 100644
--- a/arch/arm64/boot/dts/rockchip/rk3328-rock64.dts
+++ b/arch/arm64/boot/dts/rockchip/rk3328-rock64.dts
@@ -132,17 +132,16 @@
assigned-clocks = <&cru SCLK_MAC2IO>, <&cru SCLK_MAC2IO_EXT>;
assigned-clock-parents = <&gmac_clkin>, <&gmac_clkin>;
clock_in_out = "input";
- /* shows instability at 1GBit right now */
- max-speed = <100>;
phy-supply = <&vcc_io>;
phy-mode = "rgmii";
pinctrl-names = "default";
pinctrl-0 = <&rgmiim1_pins>;
+ snps,force_thresh_dma_mode;
snps,reset-gpio = <&gpio1 RK_PC2 GPIO_ACTIVE_LOW>;
snps,reset-active-low;
snps,reset-delays-us = <0 10000 50000>;
- tx_delay = <0x26>;
- rx_delay = <0x11>;
+ tx_delay = <0x24>;
+ rx_delay = <0x18>;
status = "okay";
};